<feed xmlns='http://www.w3.org/2005/Atom'>
<title>linux-toradex.git/drivers/bluetooth, branch v4.9.100</title>
<subtitle>Linux kernel for Apalis and Colibri modules</subtitle>
<link rel='alternate' type='text/html' href='https://git.toradex.cn/cgit/linux-toradex.git/'/>
<entry>
<title>Revert "Bluetooth: btusb: Fix quirk for Atheros 1525/QCA6174"</title>
<updated>2018-05-16T08:08:44+00:00</updated>
<author>
<name>Hans de Goede</name>
<email>hdegoede@redhat.com</email>
</author>
<published>2018-04-26T12:18:19+00:00</published>
<link rel='alternate' type='text/html' href='https://git.toradex.cn/cgit/linux-toradex.git/commit/?id=c7a2c159d6beff177aa9df5037b30a5a9ec08d1b'/>
<id>c7a2c159d6beff177aa9df5037b30a5a9ec08d1b</id>
<content type='text'>
commit 544a591668813583021474fa5c7ff4942244d654 upstream.

Commit f44cb4b19ed4 ("Bluetooth: btusb: Fix quirk for Atheros
1525/QCA6174") is causing bluetooth to no longer work for several
people, see: https://bugzilla.redhat.com/show_bug.cgi?id=1568911

So lets revert it for now and try to find another solution for
devices which need the modified quirk.

Cc: stable@vger.kernel.org
Cc: Takashi Iwai &lt;tiwai@suse.de&gt;
Signed-off-by: Hans de Goede &lt;hdegoede@redhat.com&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
commit 544a591668813583021474fa5c7ff4942244d654 upstream.

Commit f44cb4b19ed4 ("Bluetooth: btusb: Fix quirk for Atheros
1525/QCA6174") is causing bluetooth to no longer work for several
people, see: https://bugzilla.redhat.com/show_bug.cgi?id=1568911

So lets revert it for now and try to find another solution for
devices which need the modified quirk.

Cc: stable@vger.kernel.org
Cc: Takashi Iwai &lt;tiwai@suse.de&gt;
Signed-off-by: Hans de Goede &lt;hdegoede@redhat.com&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
<entry>
<title>Bluetooth: btusb: Fix quirk for Atheros 1525/QCA6174</title>
<updated>2018-03-28T16:39:20+00:00</updated>
<author>
<name>Takashi Iwai</name>
<email>tiwai@suse.de</email>
</author>
<published>2018-03-15T16:02:34+00:00</published>
<link rel='alternate' type='text/html' href='https://git.toradex.cn/cgit/linux-toradex.git/commit/?id=dd62bc3058313ef183aeb22d9de2297cb486dd8d'/>
<id>dd62bc3058313ef183aeb22d9de2297cb486dd8d</id>
<content type='text'>
commit f44cb4b19ed40b655c2d422c9021ab2c2625adb6 upstream.

The Atheros 1525/QCA6174 BT doesn't seem working properly on the
recent kernels, as it tries to load a wrong firmware
ar3k/AthrBT_0x00000200.dfu and it fails.

This seems to have been a problem for some time, and the known
workaround is to apply BTUSB_QCA_ROM quirk instead of BTUSB_ATH3012.

The device in question is:

T: Bus=01 Lev=01 Prnt=01 Port=09 Cnt=03 Dev#=  4 Spd=12   MxCh= 0
D: Ver= 1.10 Cls=e0(wlcon) Sub=01 Prot=01 MxPS=64 #Cfgs=  1
P: Vendor=0cf3 ProdID=3004 Rev= 0.01
C:* #Ifs= 2 Cfg#= 1 Atr=e0 MxPwr=100mA
I:* If#= 0 Alt= 0 #EPs= 3 Cls=e0(wlcon) Sub=01 Prot=01 Driver=btusb
E: Ad=81(I) Atr=03(Int.) MxPS=  16 Ivl=1ms
E: Ad=82(I) Atr=02(Bulk) MxPS=  64 Ivl=0ms
E: Ad=02(O) Atr=02(Bulk) MxPS=  64 Ivl=0ms
I:* If#= 1 Alt= 0 #EPs= 2 Cls=e0(wlcon) Sub=01 Prot=01 Driver=btusb
E: Ad=83(I) Atr=01(Isoc) MxPS=   0 Ivl=1ms
E: Ad=03(O) Atr=01(Isoc) MxPS=   0 Ivl=1ms
I: If#= 1 Alt= 1 #EPs= 2 Cls=e0(wlcon) Sub=01 Prot=01 Driver=btusb
E: Ad=83(I) Atr=01(Isoc) MxPS=   9 Ivl=1ms
E: Ad=03(O) Atr=01(Isoc) MxPS=   9 Ivl=1ms
I: If#= 1 Alt= 2 #EPs= 2 Cls=e0(wlcon) Sub=01 Prot=01 Driver=btusb
E: Ad=83(I) Atr=01(Isoc) MxPS=  17 Ivl=1ms
E: Ad=03(O) Atr=01(Isoc) MxPS=  17 Ivl=1ms
I: If#= 1 Alt= 3 #EPs= 2 Cls=e0(wlcon) Sub=01 Prot=01 Driver=btusb
E: Ad=83(I) Atr=01(Isoc) MxPS=  25 Ivl=1ms
E: Ad=03(O) Atr=01(Isoc) MxPS=  25 Ivl=1ms
I: If#= 1 Alt= 4 #EPs= 2 Cls=e0(wlcon) Sub=01 Prot=01 Driver=btusb
E: Ad=83(I) Atr=01(Isoc) MxPS=  33 Ivl=1ms
E: Ad=03(O) Atr=01(Isoc) MxPS=  33 Ivl=1ms
I: If#= 1 Alt= 5 #EPs= 2 Cls=e0(wlcon) Sub=01 Prot=01 Driver=btusb
E: Ad=83(I) Atr=01(Isoc) MxPS=  49 Ivl=1ms
E: Ad=03(O) Atr=01(Isoc) MxPS=  49 Ivl=1ms

Bugzilla: http://bugzilla.opensuse.org/show_bug.cgi?id=1082504
Reported-by: Ivan Levshin &lt;ivan.levshin@microfocus.com&gt;
Tested-by: Ivan Levshin &lt;ivan.levshin@microfocus.com&gt;
Cc: &lt;stable@vger.kernel.org&gt;
Signed-off-by: Takashi Iwai &lt;tiwai@suse.de&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
commit f44cb4b19ed40b655c2d422c9021ab2c2625adb6 upstream.

The Atheros 1525/QCA6174 BT doesn't seem working properly on the
recent kernels, as it tries to load a wrong firmware
ar3k/AthrBT_0x00000200.dfu and it fails.

This seems to have been a problem for some time, and the known
workaround is to apply BTUSB_QCA_ROM quirk instead of BTUSB_ATH3012.

The device in question is:

T: Bus=01 Lev=01 Prnt=01 Port=09 Cnt=03 Dev#=  4 Spd=12   MxCh= 0
D: Ver= 1.10 Cls=e0(wlcon) Sub=01 Prot=01 MxPS=64 #Cfgs=  1
P: Vendor=0cf3 ProdID=3004 Rev= 0.01
C:* #Ifs= 2 Cfg#= 1 Atr=e0 MxPwr=100mA
I:* If#= 0 Alt= 0 #EPs= 3 Cls=e0(wlcon) Sub=01 Prot=01 Driver=btusb
E: Ad=81(I) Atr=03(Int.) MxPS=  16 Ivl=1ms
E: Ad=82(I) Atr=02(Bulk) MxPS=  64 Ivl=0ms
E: Ad=02(O) Atr=02(Bulk) MxPS=  64 Ivl=0ms
I:* If#= 1 Alt= 0 #EPs= 2 Cls=e0(wlcon) Sub=01 Prot=01 Driver=btusb
E: Ad=83(I) Atr=01(Isoc) MxPS=   0 Ivl=1ms
E: Ad=03(O) Atr=01(Isoc) MxPS=   0 Ivl=1ms
I: If#= 1 Alt= 1 #EPs= 2 Cls=e0(wlcon) Sub=01 Prot=01 Driver=btusb
E: Ad=83(I) Atr=01(Isoc) MxPS=   9 Ivl=1ms
E: Ad=03(O) Atr=01(Isoc) MxPS=   9 Ivl=1ms
I: If#= 1 Alt= 2 #EPs= 2 Cls=e0(wlcon) Sub=01 Prot=01 Driver=btusb
E: Ad=83(I) Atr=01(Isoc) MxPS=  17 Ivl=1ms
E: Ad=03(O) Atr=01(Isoc) MxPS=  17 Ivl=1ms
I: If#= 1 Alt= 3 #EPs= 2 Cls=e0(wlcon) Sub=01 Prot=01 Driver=btusb
E: Ad=83(I) Atr=01(Isoc) MxPS=  25 Ivl=1ms
E: Ad=03(O) Atr=01(Isoc) MxPS=  25 Ivl=1ms
I: If#= 1 Alt= 4 #EPs= 2 Cls=e0(wlcon) Sub=01 Prot=01 Driver=btusb
E: Ad=83(I) Atr=01(Isoc) MxPS=  33 Ivl=1ms
E: Ad=03(O) Atr=01(Isoc) MxPS=  33 Ivl=1ms
I: If#= 1 Alt= 5 #EPs= 2 Cls=e0(wlcon) Sub=01 Prot=01 Driver=btusb
E: Ad=83(I) Atr=01(Isoc) MxPS=  49 Ivl=1ms
E: Ad=03(O) Atr=01(Isoc) MxPS=  49 Ivl=1ms

Bugzilla: http://bugzilla.opensuse.org/show_bug.cgi?id=1082504
Reported-by: Ivan Levshin &lt;ivan.levshin@microfocus.com&gt;
Tested-by: Ivan Levshin &lt;ivan.levshin@microfocus.com&gt;
Cc: &lt;stable@vger.kernel.org&gt;
Signed-off-by: Takashi Iwai &lt;tiwai@suse.de&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
<entry>
<title>Bluetooth: btqcomsmd: Fix skb double free corruption</title>
<updated>2018-03-24T10:00:22+00:00</updated>
<author>
<name>Loic Poulain</name>
<email>loic.poulain@linaro.org</email>
</author>
<published>2017-11-22T14:03:17+00:00</published>
<link rel='alternate' type='text/html' href='https://git.toradex.cn/cgit/linux-toradex.git/commit/?id=dadb6c1a8d889b5cab5ff6ed44db9cdb445467e7'/>
<id>dadb6c1a8d889b5cab5ff6ed44db9cdb445467e7</id>
<content type='text'>
[ Upstream commit 67b8fbead4685b36d290a0ef91c6ddffc4920ec9 ]

In case of hci send frame failure, skb is still owned
by the caller (hci_core) and then should not be freed.

This fixes crash on dragonboard-410c when sending SCO
packet. skb is freed by both btqcomsmd and hci_core.

Fixes: 1511cc750c3d ("Bluetooth: Introduce Qualcomm WCNSS SMD based HCI driver")
Signed-off-by: Loic Poulain &lt;loic.poulain@linaro.org&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Sasha Levin &lt;alexander.levin@microsoft.com&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
[ Upstream commit 67b8fbead4685b36d290a0ef91c6ddffc4920ec9 ]

In case of hci send frame failure, skb is still owned
by the caller (hci_core) and then should not be freed.

This fixes crash on dragonboard-410c when sending SCO
packet. skb is freed by both btqcomsmd and hci_core.

Fixes: 1511cc750c3d ("Bluetooth: Introduce Qualcomm WCNSS SMD based HCI driver")
Signed-off-by: Loic Poulain &lt;loic.poulain@linaro.org&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Sasha Levin &lt;alexander.levin@microsoft.com&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
</pre>
</div>
</content>
</entry>
<entry>
<title>Bluetooth: hci_qca: Avoid setup failure on missing rampatch</title>
<updated>2018-03-24T10:00:22+00:00</updated>
<author>
<name>Loic Poulain</name>
<email>loic.poulain@linaro.org</email>
</author>
<published>2017-11-06T11:16:56+00:00</published>
<link rel='alternate' type='text/html' href='https://git.toradex.cn/cgit/linux-toradex.git/commit/?id=f37dc00bace9e9deb2c3db35fc7bf815dbf0c913'/>
<id>f37dc00bace9e9deb2c3db35fc7bf815dbf0c913</id>
<content type='text'>
[ Upstream commit ba8f3597900291a93604643017fff66a14546015 ]

Assuming that the original code idea was to enable in-band sleeping
only if the setup_rome method returns succes and run in 'standard'
mode otherwise, we should not return setup_rome return value which
makes qca_setup fail if no rampatch/nvm file found.

This fixes BT issue on the dragonboard-820C p4 which includes the
following QCA controller:
hci0: Product:0x00000008
hci0: Patch  :0x00000111
hci0: ROM    :0x00000302
hci0: SOC    :0x00000044

Since there is no rampatch for this controller revision, just make
it work as is.

Signed-off-by: Loic Poulain &lt;loic.poulain@linaro.org&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Sasha Levin &lt;alexander.levin@microsoft.com&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
[ Upstream commit ba8f3597900291a93604643017fff66a14546015 ]

Assuming that the original code idea was to enable in-band sleeping
only if the setup_rome method returns succes and run in 'standard'
mode otherwise, we should not return setup_rome return value which
makes qca_setup fail if no rampatch/nvm file found.

This fixes BT issue on the dragonboard-820C p4 which includes the
following QCA controller:
hci0: Product:0x00000008
hci0: Patch  :0x00000111
hci0: ROM    :0x00000302
hci0: SOC    :0x00000044

Since there is no rampatch for this controller revision, just make
it work as is.

Signed-off-by: Loic Poulain &lt;loic.poulain@linaro.org&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Sasha Levin &lt;alexander.levin@microsoft.com&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
</pre>
</div>
</content>
</entry>
<entry>
<title>Bluetooth: hci_ldisc: Add protocol check to hci_uart_tx_wakeup()</title>
<updated>2018-03-24T10:00:19+00:00</updated>
<author>
<name>Dean Jenkins</name>
<email>Dean_Jenkins@mentor.com</email>
</author>
<published>2017-04-28T12:57:26+00:00</published>
<link rel='alternate' type='text/html' href='https://git.toradex.cn/cgit/linux-toradex.git/commit/?id=b5d95e85b20634f58c2d57f4041222a9adefd282'/>
<id>b5d95e85b20634f58c2d57f4041222a9adefd282</id>
<content type='text'>
[ Upstream commit 2d6f1da168e1d62c47f7d50135ac4cbd8411dcb1 ]

Before attempting to schedule a work-item onto hu-&gt;write_work in
hci_uart_tx_wakeup(), check that the Data Link protocol layer is
still bound to the HCI UART driver.

Failure to perform this protocol check causes a race condition between
the work queue hu-&gt;write_work running hci_uart_write_work() and the
Data Link protocol layer being unbound (closed) in hci_uart_tty_close().

Note hci_uart_tty_close() does have a "cancel_work_sync(&amp;hu-&gt;write_work)"
but it is ineffective because it cannot prevent work-items being added
to hu-&gt;write_work after cancel_work_sync() has run.

Therefore, add a check for HCI_UART_PROTO_READY into hci_uart_tx_wakeup()
which prevents scheduling of the work queue when HCI_UART_PROTO_READY
is in the clear state. However, note a small race condition remains
because the hci_uart_tx_wakeup() thread can run in parallel with the
hci_uart_tty_close() thread so it is possible that a schedule of
hu-&gt;write_work can occur when HCI_UART_PROTO_READY is cleared. A complete
solution needs locking of the threads which is implemented in a future
commit.

Signed-off-by: Dean Jenkins &lt;Dean_Jenkins@mentor.com&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Sasha Levin &lt;alexander.levin@microsoft.com&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
[ Upstream commit 2d6f1da168e1d62c47f7d50135ac4cbd8411dcb1 ]

Before attempting to schedule a work-item onto hu-&gt;write_work in
hci_uart_tx_wakeup(), check that the Data Link protocol layer is
still bound to the HCI UART driver.

Failure to perform this protocol check causes a race condition between
the work queue hu-&gt;write_work running hci_uart_write_work() and the
Data Link protocol layer being unbound (closed) in hci_uart_tty_close().

Note hci_uart_tty_close() does have a "cancel_work_sync(&amp;hu-&gt;write_work)"
but it is ineffective because it cannot prevent work-items being added
to hu-&gt;write_work after cancel_work_sync() has run.

Therefore, add a check for HCI_UART_PROTO_READY into hci_uart_tx_wakeup()
which prevents scheduling of the work queue when HCI_UART_PROTO_READY
is in the clear state. However, note a small race condition remains
because the hci_uart_tx_wakeup() thread can run in parallel with the
hci_uart_tty_close() thread so it is possible that a schedule of
hu-&gt;write_work can occur when HCI_UART_PROTO_READY is cleared. A complete
solution needs locking of the threads which is implemented in a future
commit.

Signed-off-by: Dean Jenkins &lt;Dean_Jenkins@mentor.com&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Sasha Levin &lt;alexander.levin@microsoft.com&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
</pre>
</div>
</content>
</entry>
<entry>
<title>Bluetooth: hci_ldisc: Add protocol check to hci_uart_dequeue()</title>
<updated>2018-03-24T10:00:19+00:00</updated>
<author>
<name>Dean Jenkins</name>
<email>Dean_Jenkins@mentor.com</email>
</author>
<published>2017-04-28T12:57:25+00:00</published>
<link rel='alternate' type='text/html' href='https://git.toradex.cn/cgit/linux-toradex.git/commit/?id=bbb952d00c8b254890e1cef7f7b7d23874c3aaa9'/>
<id>bbb952d00c8b254890e1cef7f7b7d23874c3aaa9</id>
<content type='text'>
[ Upstream commit 048e1bd3a27fbeb84ccdff52e165370c1339a193 ]

Before attempting to dequeue a Data Link protocol encapsulated message,
check that the Data Link protocol is still bound to the HCI UART driver.
This makes the code consistent with the usage of the other proto
function pointers.

Therefore, add a check for HCI_UART_PROTO_READY into hci_uart_dequeue()
and return NULL if the Data Link protocol is not bound.

This is needed for robustness as there is a scheduling race condition.
hci_uart_write_work() is scheduled to run via work queue hu-&gt;write_work
from hci_uart_tx_wakeup(). Therefore, there is a delay between
scheduling hci_uart_write_work() to run and hci_uart_dequeue() running
whereby the Data Link protocol layer could become unbound during the
scheduling delay. In this case, without the check, the call to the
unbound Data Link protocol layer dequeue function can crash.

It is noted that hci_uart_tty_close() has a
"cancel_work_sync(&amp;hu-&gt;write_work)" statement but this only reduces
the window of the race condition because it is possible for a new
work-item to be added to work queue hu-&gt;write_work after the call to
cancel_work_sync(). For example, Data Link layer retransmissions can
be added to the work queue after the cancel_work_sync() has finished.

Signed-off-by: Dean Jenkins &lt;Dean_Jenkins@mentor.com&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Sasha Levin &lt;alexander.levin@microsoft.com&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
[ Upstream commit 048e1bd3a27fbeb84ccdff52e165370c1339a193 ]

Before attempting to dequeue a Data Link protocol encapsulated message,
check that the Data Link protocol is still bound to the HCI UART driver.
This makes the code consistent with the usage of the other proto
function pointers.

Therefore, add a check for HCI_UART_PROTO_READY into hci_uart_dequeue()
and return NULL if the Data Link protocol is not bound.

This is needed for robustness as there is a scheduling race condition.
hci_uart_write_work() is scheduled to run via work queue hu-&gt;write_work
from hci_uart_tx_wakeup(). Therefore, there is a delay between
scheduling hci_uart_write_work() to run and hci_uart_dequeue() running
whereby the Data Link protocol layer could become unbound during the
scheduling delay. In this case, without the check, the call to the
unbound Data Link protocol layer dequeue function can crash.

It is noted that hci_uart_tty_close() has a
"cancel_work_sync(&amp;hu-&gt;write_work)" statement but this only reduces
the window of the race condition because it is possible for a new
work-item to be added to work queue hu-&gt;write_work after the call to
cancel_work_sync(). For example, Data Link layer retransmissions can
be added to the work queue after the cancel_work_sync() has finished.

Signed-off-by: Dean Jenkins &lt;Dean_Jenkins@mentor.com&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Sasha Levin &lt;alexander.levin@microsoft.com&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
</pre>
</div>
</content>
</entry>
<entry>
<title>Bluetooth: btusb: Restore QCA Rome suspend/resume fix with a "rewritten" version</title>
<updated>2018-02-17T12:21:19+00:00</updated>
<author>
<name>Hans de Goede</name>
<email>hdegoede@redhat.com</email>
</author>
<published>2018-01-08T09:44:16+00:00</published>
<link rel='alternate' type='text/html' href='https://git.toradex.cn/cgit/linux-toradex.git/commit/?id=5795b076bd7f98fc80ce088f8f79bbe02e2553ca'/>
<id>5795b076bd7f98fc80ce088f8f79bbe02e2553ca</id>
<content type='text'>
commit 61f5acea8737d9b717fcc22bb6679924f3c82b98 upstream.

Commit 7d06d5895c15 ("Revert "Bluetooth: btusb: fix QCA...suspend/resume"")
removed the setting of the BTUSB_RESET_RESUME quirk for QCA Rome devices,
instead favoring adding USB_QUIRK_RESET_RESUME quirks in usb/core/quirks.c.

This was done because the DIY BTUSB_RESET_RESUME reset-resume handling
has several issues (see the original commit message). An added advantage
of moving over to the USB-core reset-resume handling is that it also
disables autosuspend for these devices, which is similarly broken on these.

But there are 2 issues with this approach:
1) It leaves the broken DIY BTUSB_RESET_RESUME code in place for Realtek
   devices.
2) Sofar only 2 of the 10 QCA devices known to the btusb code have been
   added to usb/core/quirks.c and if we fix the Realtek case the same way
   we need to add an additional 14 entries. So in essence we need to
   duplicate a large part of the usb_device_id table in btusb.c in
   usb/core/quirks.c and manually keep them in sync.

This commit instead restores setting a reset-resume quirk for QCA devices
in the btusb.c code, avoiding the duplicate usb_device_id table problem.

This commit avoids the problems with the original DIY BTUSB_RESET_RESUME
code by simply setting the USB_QUIRK_RESET_RESUME quirk directly on the
usb_device.

This commit also moves the BTUSB_REALTEK case over to directly setting the
USB_QUIRK_RESET_RESUME on the usb_device and removes the now unused
BTUSB_RESET_RESUME code.

BugLink: https://bugzilla.redhat.com/show_bug.cgi?id=1514836
Fixes: 7d06d5895c15 ("Revert "Bluetooth: btusb: fix QCA...suspend/resume"")
Cc: Leif Liddy &lt;leif.linux@gmail.com&gt;
Cc: Matthias Kaehlcke &lt;mka@chromium.org&gt;
Cc: Brian Norris &lt;briannorris@chromium.org&gt;
Cc: Daniel Drake &lt;drake@endlessm.com&gt;
Cc: Kai-Heng Feng &lt;kai.heng.feng@canonical.com&gt;
Signed-off-by: Hans de Goede &lt;hdegoede@redhat.com&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
commit 61f5acea8737d9b717fcc22bb6679924f3c82b98 upstream.

Commit 7d06d5895c15 ("Revert "Bluetooth: btusb: fix QCA...suspend/resume"")
removed the setting of the BTUSB_RESET_RESUME quirk for QCA Rome devices,
instead favoring adding USB_QUIRK_RESET_RESUME quirks in usb/core/quirks.c.

This was done because the DIY BTUSB_RESET_RESUME reset-resume handling
has several issues (see the original commit message). An added advantage
of moving over to the USB-core reset-resume handling is that it also
disables autosuspend for these devices, which is similarly broken on these.

But there are 2 issues with this approach:
1) It leaves the broken DIY BTUSB_RESET_RESUME code in place for Realtek
   devices.
2) Sofar only 2 of the 10 QCA devices known to the btusb code have been
   added to usb/core/quirks.c and if we fix the Realtek case the same way
   we need to add an additional 14 entries. So in essence we need to
   duplicate a large part of the usb_device_id table in btusb.c in
   usb/core/quirks.c and manually keep them in sync.

This commit instead restores setting a reset-resume quirk for QCA devices
in the btusb.c code, avoiding the duplicate usb_device_id table problem.

This commit avoids the problems with the original DIY BTUSB_RESET_RESUME
code by simply setting the USB_QUIRK_RESET_RESUME quirk directly on the
usb_device.

This commit also moves the BTUSB_REALTEK case over to directly setting the
USB_QUIRK_RESET_RESUME on the usb_device and removes the now unused
BTUSB_RESET_RESUME code.

BugLink: https://bugzilla.redhat.com/show_bug.cgi?id=1514836
Fixes: 7d06d5895c15 ("Revert "Bluetooth: btusb: fix QCA...suspend/resume"")
Cc: Leif Liddy &lt;leif.linux@gmail.com&gt;
Cc: Matthias Kaehlcke &lt;mka@chromium.org&gt;
Cc: Brian Norris &lt;briannorris@chromium.org&gt;
Cc: Daniel Drake &lt;drake@endlessm.com&gt;
Cc: Kai-Heng Feng &lt;kai.heng.feng@canonical.com&gt;
Signed-off-by: Hans de Goede &lt;hdegoede@redhat.com&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
<entry>
<title>Revert "Bluetooth: btusb: fix QCA Rome suspend/resume"</title>
<updated>2018-02-17T12:21:19+00:00</updated>
<author>
<name>Kai-Heng Feng</name>
<email>kai.heng.feng@canonical.com</email>
</author>
<published>2017-12-20T11:00:07+00:00</published>
<link rel='alternate' type='text/html' href='https://git.toradex.cn/cgit/linux-toradex.git/commit/?id=84bf682f53422a08086dd3f1b0db1dbda46fead3'/>
<id>84bf682f53422a08086dd3f1b0db1dbda46fead3</id>
<content type='text'>
commit 7d06d5895c159f64c46560dc258e553ad8670fe0 upstream.

This reverts commit fd865802c66bc451dc515ed89360f84376ce1a56.

This commit causes a regression on some QCA ROME chips. The USB device
reset happens in btusb_open(), hence firmware loading gets interrupted.

Furthermore, this commit stops working after commit
("a0085f2510e8976614ad8f766b209448b385492f Bluetooth: btusb: driver to
enable the usb-wakeup feature"). Reset-resume quirk only gets enabled in
btusb_suspend() when it's not a wakeup source.

If we really want to reset the USB device, we need to do it before
btusb_open(). Let's handle it in drivers/usb/core/quirks.c.

Cc: Leif Liddy &lt;leif.linux@gmail.com&gt;
Cc: Matthias Kaehlcke &lt;mka@chromium.org&gt;
Cc: Brian Norris &lt;briannorris@chromium.org&gt;
Cc: Daniel Drake &lt;drake@endlessm.com&gt;
Signed-off-by: Kai-Heng Feng &lt;kai.heng.feng@canonical.com&gt;
Reviewed-by: Brian Norris &lt;briannorris@chromium.org&gt;
Tested-by: Brian Norris &lt;briannorris@chromium.org&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
commit 7d06d5895c159f64c46560dc258e553ad8670fe0 upstream.

This reverts commit fd865802c66bc451dc515ed89360f84376ce1a56.

This commit causes a regression on some QCA ROME chips. The USB device
reset happens in btusb_open(), hence firmware loading gets interrupted.

Furthermore, this commit stops working after commit
("a0085f2510e8976614ad8f766b209448b385492f Bluetooth: btusb: driver to
enable the usb-wakeup feature"). Reset-resume quirk only gets enabled in
btusb_suspend() when it's not a wakeup source.

If we really want to reset the USB device, we need to do it before
btusb_open(). Let's handle it in drivers/usb/core/quirks.c.

Cc: Leif Liddy &lt;leif.linux@gmail.com&gt;
Cc: Matthias Kaehlcke &lt;mka@chromium.org&gt;
Cc: Brian Norris &lt;briannorris@chromium.org&gt;
Cc: Daniel Drake &lt;drake@endlessm.com&gt;
Signed-off-by: Kai-Heng Feng &lt;kai.heng.feng@canonical.com&gt;
Reviewed-by: Brian Norris &lt;briannorris@chromium.org&gt;
Tested-by: Brian Norris &lt;briannorris@chromium.org&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
<entry>
<title>Bluetooth: btsdio: Do not bind to non-removable BCM43341</title>
<updated>2018-02-17T12:21:18+00:00</updated>
<author>
<name>Hans de Goede</name>
<email>hdegoede@redhat.com</email>
</author>
<published>2017-11-29T19:29:07+00:00</published>
<link rel='alternate' type='text/html' href='https://git.toradex.cn/cgit/linux-toradex.git/commit/?id=6913d1b190b99855b740f648ea70cede43e52eff'/>
<id>6913d1b190b99855b740f648ea70cede43e52eff</id>
<content type='text'>
commit b4cdaba274247c9c841c6a682c08fa91fb3aa549 upstream.

BCM43341 devices soldered onto the PCB (non-removable) always (AFAICT)
use an UART connection for bluetooth. But they also advertise btsdio
support on their 3th sdio function, this causes 2 problems:

1) A non functioning BT HCI getting registered

2) Since the btsdio driver does not have suspend/resume callbacks,
mmc_sdio_pre_suspend will return -ENOSYS, causing mmc_pm_notify()
to react as if the SDIO-card is removed and since the slot is
marked as non-removable it will never get detected as inserted again.
Which results in wifi no longer working after a suspend/resume.

This commit fixes both by making btsdio ignore BCM43341 devices
when connected to a slot which is marked non-removable.

Signed-off-by: Hans de Goede &lt;hdegoede@redhat.com&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
commit b4cdaba274247c9c841c6a682c08fa91fb3aa549 upstream.

BCM43341 devices soldered onto the PCB (non-removable) always (AFAICT)
use an UART connection for bluetooth. But they also advertise btsdio
support on their 3th sdio function, this causes 2 problems:

1) A non functioning BT HCI getting registered

2) Since the btsdio driver does not have suspend/resume callbacks,
mmc_sdio_pre_suspend will return -ENOSYS, causing mmc_pm_notify()
to react as if the SDIO-card is removed and since the slot is
marked as non-removable it will never get detected as inserted again.
Which results in wifi no longer working after a suspend/resume.

This commit fixes both by making btsdio ignore BCM43341 devices
when connected to a slot which is marked non-removable.

Signed-off-by: Hans de Goede &lt;hdegoede@redhat.com&gt;
Signed-off-by: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
<entry>
<title>Revert "Bluetooth: btusb: driver to enable the usb-wakeup feature"</title>
<updated>2017-12-25T13:23:46+00:00</updated>
<author>
<name>Greg Kroah-Hartman</name>
<email>gregkh@linuxfoundation.org</email>
</author>
<published>2017-12-22T07:43:23+00:00</published>
<link rel='alternate' type='text/html' href='https://git.toradex.cn/cgit/linux-toradex.git/commit/?id=3b6c84bc64490529c33bd5f0f9e2c6256031f398'/>
<id>3b6c84bc64490529c33bd5f0f9e2c6256031f398</id>
<content type='text'>
This reverts commit 7336f5481f6cf913a2d29d98c6e11f4bbe19d3b2 which is
commit a0085f2510e8976614ad8f766b209448b385492f upstream.

It causes problems with working systems, as noted by a number of the
ChromeOS developers.

Cc: Sukumar Ghorai &lt;sukumar.ghorai@intel.com&gt;
Cc: Amit K Bag &lt;amit.k.bag@intel.com&gt;
Cc: Oliver Neukum &lt;oneukum@suse.com&gt;
Cc: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Cc: Matthias Kaehlcke &lt;mka@chromium.org&gt;
Reported-by: Guenter Roeck &lt;linux@roeck-us.net&gt;
Reported-by: Brian Norris &lt;briannorris@chromium.org&gt;
Acked-by: Brian Norris &lt;briannorris@chromium.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
This reverts commit 7336f5481f6cf913a2d29d98c6e11f4bbe19d3b2 which is
commit a0085f2510e8976614ad8f766b209448b385492f upstream.

It causes problems with working systems, as noted by a number of the
ChromeOS developers.

Cc: Sukumar Ghorai &lt;sukumar.ghorai@intel.com&gt;
Cc: Amit K Bag &lt;amit.k.bag@intel.com&gt;
Cc: Oliver Neukum &lt;oneukum@suse.com&gt;
Cc: Marcel Holtmann &lt;marcel@holtmann.org&gt;
Cc: Matthias Kaehlcke &lt;mka@chromium.org&gt;
Reported-by: Guenter Roeck &lt;linux@roeck-us.net&gt;
Reported-by: Brian Norris &lt;briannorris@chromium.org&gt;
Acked-by: Brian Norris &lt;briannorris@chromium.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
</pre>
</div>
</content>
</entry>
</feed>
